ASN Wikibase Occurrence # 383287
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 19 September 1982 |
Time: | 12:50 LT |
Type: | Thurston TSC-1A |
Owner/operator: | Richard Callis |
Registration: | N2019T |
MSN: | 19 |
Total airframe hrs: | 605 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Homer, AK -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Homer, AK |
Destination airport: | Homer, AK |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A WATER TAKEOFF, THE AIRCRAFT IMPACTED A LARGE WAVE UNEXPECTEDLY. WITNESSES STATED THAT THE AIRCRAFT WAS THROWN TO A HEIGHT OF APPROXIMATELY 12 FEET. THE PILOT STATED THAT THE AIRSPEED WAS ABOUT 40 TO 45 KNOT'S AT THE TIME OF IMPACT WITH THE WAVE. HE PULLED THE THROTTLE CLOSED AND RELEASED ELEVATOR BACK PRESSURE. THE AIRCRAFT REACTED AND IMPACTED THE WATER IN A NOSE LOW ATTITUDE AND NOSED OVER. THE PILOT ALSO STATED THAT THE WATER WAS GLITTERY AND UNIFORM AT THE TIME OF TAKEOFF. IT WAS LATER REVEALED THAT A LARGE, FAST BOAT HAD CROSSED THE INTENDED TAKEOFF PATH BEHIND N2019T DURING THEIR WATER TAXI. THE PILOT DID NOT OBSERVE ANY BOAT TRAFFIC PRIOR TO TAKEOFF.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC82DAG58 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ANC82DAG58
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 23:02 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation