ASN Wikibase Occurrence # 383318
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Date: | Wednesday 15 September 1982 |
Time: | 11:30 LT |
Type: | Cessna 172F |
Owner/operator: | Private |
Registration: | N8423U |
MSN: | 17252323 |
Year of manufacture: | 1964 |
Total airframe hrs: | 2259 hours |
Engine model: | Continental O-300-D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Millry, AL -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | , AL (KMOB) |
Destination airport: | (23A) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT EXPERIENCED A PARTIAL LOSS OF POWER DURING A FERRY FLIGHT AND WAS FORCED TO MAKE AN EMERGENCY LANDING IN A FIELD. HE STATED THAT HE NOTED 4 VIBRATIONS FOLLOWED BY A MISSING IN THE ENGINE. THE RPM DROPPED TO 1200 AND HE COULD NOT MAINTAIN ALTITUDE. OCCASIONALLY, BY PUMPING THE THROTTLE HE WAS ABLE TO INCREASE THE RPM ABOVE 1200. EXAMINATION REVEALED A SEPARATION OF THE RIGHT EXHAUST FLAME TUBE WHICH SUBSEQUENTLY CAUSED A POWER LOSS.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL82DA275 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ATL82DA275
Location
Revision history:
Date/time | Contributor | Updates |
02-Apr-2024 23:21 |
ASN Update Bot |
Added |
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