ASN Wikibase Occurrence # 383489
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 25 August 1982 |
Time: | 10:20 LT |
Type: | Cessna 421C |
Owner/operator: | Richmor Aviation |
Registration: | N88572 |
MSN: | 421C0637 |
Total airframe hrs: | 893 hours |
Engine model: | Continental GTSIO-520-L |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Saratoga Spring, NY -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Hudson, NY (1B1) |
Destination airport: | Saratoga Spring, NY |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT WAS ON A FLIGHT TO REPOSITION IT FOR AN AIR TAXI OPERATION. THE PILOT-IN-COMMAND (PIC) WAS IN THE RIGHT SEAT WHILE THE SECOND-IN-COMMAND (SIC) WAS FLYING IN THE LEFT SEAT. DURING ARRIVAL TO THE SARATOGA COUNTY AIRPORT, THE AIRCREW WERE CLEARED FOR THE VOR-A APPROACH. ACCORDING TO THE PIC, WHEN THEY ARRIVED AT THE GILLA INTERSECTION AND STARTED TO PROCEED OUTBOUND, THUNDERSTORM ACTIVITY WAS OBSERVED ON THE PROCEDURE TURN (SOUTH) SIDE OF THE RADIAL. THEREFORE, THEY ELECTED TO MAKE A COURSE REVERSAL ON THE NORTH SIDE. DUE TO MODERATE TO HEAVY TURBULENCE, THE PIC WAS DISTRACTED AND WAS NOT SURE IF HE SET IN THE CORRECT INBOUND HEADING. AFTER INTERCEPTING WHAT THEY THOUGHT WAS THE PROPER INBOUND RADIAL, A DESCENT WAS STARTED. JUST AFTER BREAKING OUT OF THE CLOUDS AT 1800 TO 1900FT, THE AIRCRAFT COLLIDED WITH TREES. A MISSED APPROACH WAS MADE AND THE AIRCREW DIVERTED TO ANOTHER AIRPORT WHERE THE NOSE GEAR COLLAPSED DURING LANDING. AFTER THE ACCIDENT, THEY WERE NOT SURE WHETHER THE DME WAS ON ALBANY OR CAMBRIDGE.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC82DA209 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB NYC82DA209
History of this aircraft
Other occurrences involving this aircraft
29 January 2022 |
N679JJ |
Private |
0 |
Addison Airport (ADS/KADS), Dallas, TX |
|
sub |
Runway excursion |
Location
Revision history:
Date/time | Contributor | Updates |
03-Apr-2024 01:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation