ASN Wikibase Occurrence # 384698
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Date: | Monday 5 April 1982 |
Time: | 19:50 LT |
Type: | Cessna A185E |
Owner/operator: | Private |
Registration: | N4745Q |
MSN: | 185-1199 |
Total airframe hrs: | 5529 hours |
Engine model: | Continental IO-520-D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Juneau, AK -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Auke Bay, AK |
Destination airport: | Farmerville, LA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING AN APPROACH TO LAND, THE PILOT OF THE AMPHIBIOUS AIRCRAFT EXTENDED THE GEAR AND PERFORMED HIS PRELANDING CHECKS. HE STATED THAT WHILE HE WAS DESCENDING, HE NOTICED AN EXCESSIVE LOSS OF ALTITUDE AND BEGAN TO ADD POWER. HOWEVER, THE ENGINE DID NOT RESPOND AND HE WAS UNABLE TO OBTAIN A RESTART. SUBSEQUENTLY, THE AIRCRAFT TOUCHED DOWN ON IN THE LIGHTING SYSTEM SHORT OF THE RUNWAY AND NOSED OVER. AN EXAMINATION REVEALED THAT THE LOW PRESSURE RELIEF VALVE ADJUSTING SCREW ON THE FUEL PUMP, PN 638154-1, WAS WORN AND RECESSED IN THE HOUSING. THE SCREW WOULD ROTATE AND VARY THE LOW PRESSURE FUEL SETTING.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC82DA031 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ANC82DA031
Location
Revision history:
Date/time | Contributor | Updates |
03-Apr-2024 13:56 |
ASN Update Bot |
Added |
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