ASN Wikibase Occurrence # 385401
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 14 December 2001 |
Time: | 06:15 LT |
Type: | McDonnell Douglas DC-8-71F |
Owner/operator: | Air Transport International |
Registration: | N825BX |
MSN: | 45978 |
Total airframe hrs: | 82406 hours |
Engine model: | General Electric CFM 56 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Anchorage, AK -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | Anchorage-Ted Stevens International Airport, AK (ANC/PANC) |
Destination airport: | Seattle/Tacoma International Airport, WA (SEA/KSEA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The crew of Douglas DC-8-71F airplane reported a partial flight control malfunction during takeoff. The captain reported that just after the airplane became airborne, the airplane rolled hard to the left. He said that he had to apply full right aileron control, in conjunction with right rudder, to keep the airplane from continuing to roll to the left. The crew immediately declared an in-flight emergency, returned to the airport using left turns only, and made an emergency, high speed landing, without the use of any wing flaps. After landing, the flight crew discovered that the left wing outboard spoiler had deployed just after takeoff. A postincident inspection revealed a broken outboard left wing spoiler retraction cable. An NTSB Metallurgist reported that a magnified optical examination of the broken cable revealed that the area adjacent to the fracture site was severely worn, and reduced in size. He added that many individual wire strands were worn to a knife-edge. The remaining broken strands appeared typical of overstress separations, with no indication of external corrosion. Currently, the subject cable is considered to be an "on condition" component, and has no required life limit assigned. In response to this incident the airplane's manufacture sent a safety notice to all DC-8 operators. In the notice, the manufacturer recommends that all operators review their maintenance procedures with respect to the scheduled inspection of all aircraft cables. A special emphasis was placed on the proper cable condition and cable routing.
Probable Cause: The asymmetrical activation of the left wing spoiler due to a broken retraction cable during takeoff. A factor associated with the incident was the operator's inadequate inspection of the cable.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC02IA007 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ANC02IA007
Location
Revision history:
Date/time | Contributor | Updates |
04-Apr-2024 18:13 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation