ASN Wikibase Occurrence # 385569
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Date: | Saturday 21 July 2001 |
Time: | 17:00 LT |
Type: | Anderson Revelation |
Owner/operator: | Private |
Registration: | N6116S |
MSN: | RE00/0001 |
Total airframe hrs: | 0 hours |
Engine model: | Rotax 618 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wautoma, WI -
United States of America
|
Phase: | Initial climb |
Nature: | Test |
Departure airport: | Wautoma, WI (Y50) |
Destination airport: | Wautoma, WI (Y50) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to the accident flight, which was the experimental homebuilt airplane's second flight since certification, the propeller was adjusted to a finer setting to achieve the desired static engine rpm. The pilot stated that after the takeoff during the accident flight, the airplane did not accelerate normally when out of ground effect and would not climb above approximately 30 feet. The pilot reported that there was not enough runway remaining to land and he started a shallow right turn to keep over the airport area. The pilot reported, "While maintaining 60 mph IAS [indicated airspeed] in a shallow bank, the wing stalled & I was unable to recover before impact with a corn field. The plane hit the ground with right wing about 30 [degrees] low and 20-30 [degrees] nose low." No anomalies were found with the airframe or its engine that could be associated with any pre-impact condition.
Probable Cause: The pilot's failure to maintain airspeed, resulting in a stall. An inadequate pitch setting of the propeller is a contributing factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01LA239 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB CHI01LA239
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 05:33 |
ASN Update Bot |
Added |
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