ASN Wikibase Occurrence # 385622
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 12 July 2001 |
Time: | 17:35 LT |
Type: | Piper PA-34-200T |
Owner/operator: | Private |
Registration: | N3054J |
MSN: | 34-79700065 |
Total airframe hrs: | 4973 hours |
Engine model: | Continental TSIO-360-EBIA |
Fatalities: | Fatalities: 0 / Occupants: 14 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Boca Raton, FL -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Boca Raton Public Airport, FL (BCT/KBCT) |
Destination airport: | Orlando Sanford International Airport, FL (SFB/KSFB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Just after takeoff the pilot reported that the left engine lost power. He checked that the mixture, propellers, and throttles were all full forward, and that the fuel selector was "on." He said, "...I checked the fuel selectors by feel only." He recycled the left engine feather control and made the decision to land gear up. He retracted the landing gear, and attempted to feather the left engine again without success. At this point he could not maintain altitude or airspeed, estimated that his altitude was "between 150-200 feet," and the airspeed had decayed to 78 knots (83 was Vmc). He elected to land on an interstate highway, before the airplane started a Vmc roll. He landed in a southerly direction on the northbound lanes of the highway, first striking a light pole with the left wing, and then seven vehicles. After coming to a stop, the two occupants evacuated the airplane after the passenger said he was "in a puddle of fuel." The pilot stated that he "..â¦reached down and moved the fuel selectors back. They were full forward in the 'on' position. I missed the 'off ' and mistakenly moved them to crossfeed as I exited the airplane." Examination of the fuel selectors at the crash site revealed that both engine fuel selectors were in the "crossfeed" position. The left engine was test run, and no discrepancies were found. Fuel was found in the left engine. The fuel was visually examined for contamination and water, none was observed. Examination of the right engine revealed, no discrepancies.
Probable Cause: A loss of engine power, and the pilot unable to feather the propeller for undetermined reasons, which resulted in a forced landing on a highway, subsequent impact with a pole and vehicles.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA01LA182 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB MIA01LA182
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 06:06 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation