ASN Wikibase Occurrence # 385696
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Date: | Wednesday 27 June 2001 |
Time: | 10:10 LT |
Type: | Beechcraft A36 |
Owner/operator: | International Flight Training Academy, Inc. |
Registration: | N808NH |
MSN: | E-2817 |
Total airframe hrs: | 3999 hours |
Engine model: | Continental IO-550B-6F |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Bakersfield, CA -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Bakersfield-Meadows Field, CA (BFL/KBFL) |
Destination airport: | Bakersfield-Meadows Field, CA (BFL/KBFL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the landing approach on an instructional flight, the certified flight instructor (CFI) initiated a go-around and experienced restricted elevator control movement. The elevator control became partially jammed in a nose low and then a nose high position. Roll and yaw control was not affected. Using considerable force, the CFI maintained airplane control and landed without additional incident. Thereafter, the airplane was inspected. Evidence of mechanical binding to the elevator pitch control cables was noted. Specifically, a screwdriver was found wedged between the nose gear actuator retract rod and the elevator control cables beneath the forward spar cover, between and under the pilots' seats. When the nose gear retracted, the nose gear actuator retract rod moved the screwdriver against the elevator control cable resulting in binding. Upon removal of the screwdriver, the elevator operation was normal. Two days prior to the incident, a contract mechanic had performed maintenance on the airplane. The maintenance required taking off the forward spar cover to allow removal and installation of a flap motor gearbox assembly and flap flex drives. Since this maintenance, the airplane had been operated 5.8 flight hours.
Probable Cause: During landing approach, mechanical binding of the elevator control cable occurred due to a contract mechanic's improper maintenance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01IA241 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX01IA241
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 06:57 |
ASN Update Bot |
Added |
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