ASN Wikibase Occurrence # 385765
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Date: | Thursday 14 June 2001 |
Time: | 13:00 LT |
Type: | Cessna 150 |
Owner/operator: | Private |
Registration: | N1525Q |
MSN: | 15072825 |
Year of manufacture: | 1971 |
Total airframe hrs: | 4931 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lincoln, ME -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Millinocket Municipal Airport, ME (KMLT) |
Destination airport: | Lincoln Regional Airport, ME (KLRG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While on final and approximately 600 feet agl, the student pilot decided that the airplane was not in a position to safely continue the approach. He initiated a go-around, selected the carburetor heat to "OFF," and applied full power. By the time the airplane was approximately half way down the runway, the pilot had retracted the flaps, and initiated a climb. A couple of seconds into the climb and without warning, the engine lost power. The pilot executed a forced landing, by making a 360 degree turn. The airplane touched down long, fast, and on the grass to the right of the runway. It then impacted some trees before coming to a stop. Examination of the airplane revealed that both fuel tanks had approximately 5 gallons of fuel. An engine run was then preformed. The engine started and ran smoothly. Engine rpm was limited to 1,200 because of propeller damage. A magneto check was preformed at 1,200 rpm, and engine rpm dropped approximately 100 rpm for both magnetos. After securing the engine, the fuel line between the gascolator and carburetor was disconnected, and the electric-driven fuel pump was activated. Initially, fuel was expelled a "normal" rate, but then slowed. The fuel flow then oscillated between "normal" and a reduced rate. The fuel screen was found absent of debris. The bowl contained fuel, and was also absent of debris or water.
Probable Cause: A loss of engine power for an undetermined reason.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC01LA149 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB NYC01LA149
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 07:41 |
ASN Update Bot |
Added |
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