ASN Wikibase Occurrence # 385768
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Date: | Thursday 14 June 2001 |
Time: | 11:30 LT |
Type: | Cessna 340A |
Owner/operator: | Aeroplane Services, Inc. |
Registration: | N820B |
MSN: | 340A-0328 |
Total airframe hrs: | 4683 hours |
Engine model: | Continental TSIO-520-NB |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lancaster, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Houston-William P. Hobby Airport, TX (HOU/KHOU) |
Destination airport: | Lancaster Regional Airport, TX (KLNC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot switched both fuel selectors from the auxiliary tanks to the main fuel tanks and started a descent by reducing power. During the descent, the right engine lost power. Subsequently, the left engine lost power. The pilot performed the emergency checklist and restarted both engines. Subsequently, the right engine again lost power. The landing gear collapsed during the single-engine landing, and the airplane exited the runway. The pilot stated that the "fuel selector valve failed to seal poppet valves internally, resulting in no fuel to right engine. Landing gear did not fully deploy on approach." Impact damage to the main landing gear assembly precluded a determination of the reason for the collapse of the landing gear; however, the motor operated when power was applied. During disassembly of the right fuel selector valve, the three Rulon-A seals were found depressed (stuck in the downed position) level with the housing, and the spring follower bushings for all three seals were missing. The fuel selector valve was re-assembled and pressure tested in accordance with manufacturer specifications. When the valve was set in the off position, leakage from the main port to the engine port was 212.904 cubic centimeters (cc) (specification 0.5 cc with 40 psig). When the valve was set in the main position, leakage from the auxiliary port to the engine port was 319.3456 cc (specification 0.5 cc with 8 psig). However, according to the manufacturer's representative, with the "right engine fuel selector valve in the right main tank position, the leakage would not prevent the right engine from operating when the fuel boost pumps were in the on position."
Probable Cause: A loss of engine power for undetermined reasons. Contributing to the accident was the collapse of the landing gear for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW01LA142 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW01LA142
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 07:42 |
ASN Update Bot |
Added |
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