Accident Consolildated-Vultee BT-13A N66791,
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ASN Wikibase Occurrence # 385906
 
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Date:Monday 14 May 2001
Time:13:55 LT
Type:Silhouette image of generic VALI model; specific model in this crash may look slightly different    
Consolildated-Vultee BT-13A
Owner/operator:Confederate Air Force
Registration: N66791
MSN: 3336
Total airframe hrs:2228 hours
Engine model:Pratt & Whitney R-985-ANI
Fatalities:Fatalities: / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Odessa, TX -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Midland International Air and Space Port, TX (MAF/KMAF)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot was undergoing his 7th hour of dual familiarization training in the airplane. The airplane approached the airport from the east, over flew the south end of the airport, and then executed a left teardrop turn to runway 34. According to witnesses at the airport, the airplane was on final approach to runway 34, approximately 150 feet agl, when they heard power applied to the engine. Subsequently, the right wing dropped, the airplane impacted the ground, contacted a steel pole, and came to a stop upright. The witness accounts and ground scars are consistent with the airplane encountering a stall. One witness, who was located on the airport, reported that at the time of the accident the wind was from the south at 10 mph. Two minutes prior to the accident, two weather observation facilities that are located 7 miles northeast and 9 miles northwest of the accident site, reported wind from 200 degrees at 13 knots and gusting to 20 knots and wind from 210 degrees at 11 knots and gusting to 19 knots, respectively. The airframe and engine were examined and no pre-impact anomalies were noted that would have precluded their operation.

Probable Cause: the pilot's failure to maintain the minimum required airspeed for flight, which resulted in a loss of control while performing a go-around. A contributing factor to the accident was the gusty tailwind condition.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW01FA117
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB FTW01FA117

Revision history:

Date/timeContributorUpdates
05-Apr-2024 09:05 ASN Update Bot Added

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