ASN Wikibase Occurrence # 385908
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Date: | Sunday 13 May 2001 |
Time: | 16:50 LT |
Type: | Beechcraft E33A |
Owner/operator: | South Bay Aviation, Inc. |
Registration: | N464SR |
MSN: | CE-275 |
Engine model: | Continental IO-520-B |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | So Lake Tahoe, CA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Lake Tahoe Airport, CA (TVL/KTVL) |
Destination airport: | San Jose-Reid-Hillview Airport, CA (RHV/KRHV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the pretakeoff check, the pilot observed that a mechanical malfunction existed with the vernier control button on the throttle knob. It had partially unscrewed. The pilot attempted to remedy the situation by screwing the knob back into place, and then he commenced the takeoff. The airplane was loaded at or within 240 pounds of its certificated maximum gross weight, and the density altitude was about 7,700 feet. The airplane accelerated, lifted off the ground, and gained about 30 feet. The pilot had not received dual instruction in the airplane in high density altitude procedures, and he was not experienced in this type of operation. Believing that the rate of climb was inhibited due to a downdraft, and with the wings rocking back and forth on the verge of stalling, the pilot retracted the landing gear in an effort at increasing the climb rate. Still dissatisfied with the airplane's inability to climb, the pilot retarded the throttle to abort the takeoff. He then tried to lower the landing gear. When the pilot attempted to increase the throttle to provide more time for the gear to extend, the throttle control knob jammed due to the improperly secured screw. The airplane impacted the runway with partially extended landing gear, and slid to a stop about 1,500 feet before reaching its departure end.
Probable Cause: The pilot's improper aircraft handling and decision to prematurely raise the landing gear during takeoff. Contributing factors were his lack of experience taking off under the high density altitude condition and his improper maintenance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01LA177 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB LAX01LA177
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 09:10 |
ASN Update Bot |
Added |
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