ASN Wikibase Occurrence # 385983
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Date: | Friday 27 April 2001 |
Time: | 17:22 LT |
Type: | Piper PA-31-350 |
Owner/operator: | American Aviation, Inc. |
Registration: | N27367 |
MSN: | 31-7852007 |
Year of manufacture: | 1977 |
Total airframe hrs: | 9236 hours |
Engine model: | Lycoming LTIO-540-J2BD |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | St. George, UT -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | Saint George Municipal Airport, UT (SGU/KSGU) |
Destination airport: | Salt Lake City International Airport, UT (SLC/KSLC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on runway 16, which is located on a narrow mesa (the surrounding terrain is 300 to 350 feet below). He said that immediately after takeoff, he experienced a loss of power on the right engine. The pilot feathered the propeller on the left engine and performed a forced landing. He had raised the landing gear with runway left to land on. The FAA Advisory Circular 61-21A, Flight Training Handbook states that the landing gear should not be raised until a safe landing can no longer be made on the remaining portion of the runway. Postaccident examination of both engines revealed no mechanical anomalies which might have affected their performance. Recovery personnel reported that both propellers were "dramatically" bent in the opposite direction of rotation. Additionally they found that the right wing root fuel sump valve was installed improperly, and was impossible to sump. When they removed the valve, they found that the fuel sample was approximately 25% water. The wind, at the time of the attempted takeoff, was 130 degrees at 21 gusting to 31 knots. The direct crosswind was calculated to be 16 knots, which was within the airplane's demonstrated crosswind limit of 20 knots.
Probable Cause: the pilot's failure to sump all the fuel drains during preflight and the subsequent loss of power in the right engine during takeoff, the pilot feathering the wrong engine's propeller during the forced landing, the pilot improperly raising the landing gear with usable runway in front of him, and lack of suitable terrain for the forced landing. Contributing factors were the water in the fuel, the terrain induced turbulent cross wind condition, and the mountainous/hilly terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN01LA093 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB DEN01LA093
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 09:55 |
ASN Update Bot |
Added |
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