ASN Wikibase Occurrence # 386310
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 13 January 2001 |
Time: | 17:30 LT |
Type: | Piper PA-22-150 |
Owner/operator: | Private |
Registration: | N3854P |
MSN: | 22-3546 |
Total airframe hrs: | 2054 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Atwater, CA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Merced-Castle AFB, CA (MER/KMER) |
Destination airport: | Merced-Castle AFB, CA (MER/KMER) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an instructional flight, the pilot handling the flight controls ground looped his airplane while landing on runway 31. Prior to the accident, the pilot had successfully performed a series of takeoffs and 3-point landings under the supervision of his flight instructor. However, a wind gust was encountered during the pilot's last landing. The pilot indicated that he was unable to maintain directional control, the airplane veered left, the right main landing gear collapsed, and the right wing contacted the runway surface and broke. The flight instructor indicated that, at the time, the wind was from the southwest at 10 knots, with 15-knot gusts. The pilot held a commercial pilot certificate and had about 5,000 hours of flight time, but only about 2 hours in his recently purchased tail wheel equipped airplane. The flight instructor, whom the pilot hired to check him out, had 3,469.7 hours of flight time. However, his flying experience in the accident airplane was 5 hours. Runway 31 is 11,802 feet long and 300 feet wide.
Probable Cause: The student's failure to maintain directional control while landing in a crosswind, his improper compensation for wind conditions, and the flight instructor's inadequate flight supervision.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01LA077 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB LAX01LA077
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 13:31 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation