ASN Wikibase Occurrence # 386316
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Date: | Tuesday 9 January 2001 |
Time: | 18:00 LT |
Type: | Nord 1101 |
Owner/operator: | Private |
Registration: | N208BF |
MSN: | 154 |
Total airframe hrs: | 3472 hours |
Engine model: | Renault 6Q10A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mckinney, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Mckinney, TX (T31) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during the takeoff/initial climb the engine "smoothly throttled back to a low power setting although throttle lever was at full position." During the ensuing forced landing in a soft field, the airplane's fuselage sustained damage. Examination of the engine revealed that the throttle linkage assembly's push/pull rod separated from the support bushing. The FAA inspector, who examined the airplane, stated that the rod end was "inadequately" engaged in the support bushing "due to improper installation."
Probable Cause: the loss of engine power during takeoff resulting from the inadequate engagement of the throttle torque tube rod end into the support bushing by unknown maintenance personnel.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW01LA047 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW01LA047
Location
Revision history:
Date/time | Contributor | Updates |
05-Apr-2024 13:31 |
ASN Update Bot |
Added |
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