ASN Wikibase Occurrence # 387013
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Date: | Saturday 18 February 2023 |
Time: | 12:00 LT |
Type: | Cessna 150L |
Owner/operator: | Aviator Air LLC |
Registration: | N6536G |
MSN: | 15072036 |
Year of manufacture: | 1970 |
Total airframe hrs: | 6060 hours |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Venus, TX -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Grand Prairie Municipal Airport, TX (KGPM) |
Destination airport: | Grand Prairie Municipal Airport, TX (KGPM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor stated that while practicing power off stalls the student pilot added engine power and was retracting the wing flaps when the engine began to lose power. The instructor took control of the airplane and scanned the engine instruments. He noted that oil temperature was in the green range and the oil pressure was 0 psi and blinking in the red. The engine lost total power and the flight instructor performed a forced landing to a field. During the landing roll out, the airplane nosed over and came to rest inverted. Substantial damage was sustained to the empennage and vertical stabilizer.
An examination of the airframe and an engine run did not detect any preimpact anomalies that would have contributed to a loss of engine power. The airplane was operating in conditions conducive to the formation of carburetor icing at glide and cruise power and serious icing at glide power. The instructor reported the use of carburetor heat during the flight training.
The reason for the loss of engine power could not be determined with the available information.
Probable Cause: The loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN23LA114 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN23LA114
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Apr-2024 08:10 |
ASN Update Bot |
Added |
28-Apr-2024 08:27 |
ASN |
Updated [Aircraft type, Narrative] |
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