Accident Champion 7GCAA N9648S,
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ASN Wikibase Occurrence # 387480
 
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Date:Saturday 12 August 2000
Time:10:30 LT
Type:Silhouette image of generic CH7B model; specific model in this crash may look slightly different    
Champion 7GCAA
Owner/operator:Private
Registration: N9648S
MSN: 61
Year of manufacture:1966
Total airframe hrs:3371 hours
Engine model:Lycoming O-320-A2B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Newell, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Red Bluff, CA (KRBL)
Destination airport:Prineville, OR (S39)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the cross-country flight, the engine lost power and the airplane force landed in an open field. On landing roll, the left main wheel struck a depression collapsing the left main landing gear. Prior to departure, during her preflight inspection, the pilot had determined that the fuel tanks were full. After about 2 hours of flight, the pilot and her pilot-rated passenger elected to divert to an intermediate destination because of up and down drafts. Shortly after contacting approach control to receive flight following to the divert airfield, the engine sputtered and quit. Several hours after the accident a sheriff's deputy arrived at the scene. He reported no evidence of fuel spillage. A recovery crew got to the airplane 5 days later. The recovery personnel discovered that the fuel tank caps were in place and fit snugly, the fuel gascolator had been broken off, the fuel valve was in the 'OFF' position, there was no evidence of fuel spillage, and 2 gallons of fuel remained in the airplane, all in the right wing tank. The spark plugs had a normal appearance, cylinder compressions were good, and the intake and exhaust systems were open. The carburetor bowl was empty. The engine appeared capable of operating. Unusable fuel for the airplane is 1 gallon. During the postcrash examination, the right fuel tank vent check valve was inoperable.

Probable Cause: A hidden depression in the ground that resulted in the collapse of the landing gear during the forced landing roll.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX00LA295
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB LAX00LA295

History of this aircraft

Other occurrences involving this aircraft
29 June 2007 N827BM Private 0 Orangeburg, South Carolina sub

Location

Revision history:

Date/timeContributorUpdates
03-May-2024 09:20 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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