ASN Wikibase Occurrence # 38902
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Date: | Friday 23 April 1999 |
Time: | 18:00 LT |
Type: | Beechcraft B95A Travel Air |
Owner/operator: | Ronald E. Pressley |
Registration: | N6600 |
MSN: | TD-506 |
Total airframe hrs: | 3042 hours |
Engine model: | Lycoming IO-360-B1B |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Fountain, FL -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Panama City, FL (KPFN) |
Destination airport: | Johnson City, TN (0A4 |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Before departure on a ferry flight, both previously damaged propellers were removed and replaced. An incorrect propeller was installed on the left position by a person with a revoked mechanic's certificate. The flight departed with full fuel tanks, all gears braced down, and no radios. After takeoff while flying with another airplane, the pilot motioned by hand signals that he needed to land. The pilot landed in a field with no flaps and after rolling approximately 300 feet, the airplane became airborne, then collided with several trees. Post accident examination revealed that the right propeller was feathered. Examination of the fuel vent system revealed all recovered fuel vents were blocked; an insect resembling a wasp was found in a section of the left fuel vent line. Examination of the flight controls, engines, and propellers revealed no evidence of pre-impact failure or mechanical malfunction. The No. 1 top spark plug of the left engine was missing. The pilot's airman certificate was suspended for 180 days in February 1996, for operating an airplane with incorrect propellers installed. The permanent maintenance records did not contain an entry that the airplane was inspected and found to be safe for the intended ferry flight.
Probable Cause: The pilot's inadequate preflight inspection of the airplane that resulted in a loss of engine power because of fuel vent blockage and his selection of unsuitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99FA140 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB MIA99FA140
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 12:43 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
08-Apr-2024 06:44 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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