Wirestrike Accident Piper PA-32R-300 N38188,
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ASN Wikibase Occurrence # 39742
 
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Date:Thursday 13 July 1995
Time:15:20 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-300
Owner/operator:Steven L. Coffey
Registration: N38188
MSN: 32R-7780402
Total airframe hrs:1340 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Hilton Head Isl, SC -   United States of America
Phase: Approach
Nature:Private
Departure airport:Knoxville, TN (KDKX)
Destination airport:(49J)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight departed Knoxville, TN, at 1220 edt with full fuel tanks. About 1 hour before the planned arrival at Hilton Head, SC, the pilot advised the FBO that the flight would be about 30 minutes late. The flight continued, and when near the airport, the pilot requested an airport advisory. He announced his intentions to enter a downwind leg and to make a long final approach to runway 3. Witnesses saw the airplane low on final approach, then observed that the airplane banked away from the airport, while descending. Subsequently, it collided with 80-foot tall trees, then a powerline, the ground, and a telephone pole. The airplane came to rest upright with the empennage separated aft of the wings. A postcrash fire destroyed the cockpit and cabin section. Examination of the flight controls revealed no evidence of preimpact failure or malfunction. Examination of the engine revealed water contamination at the fuel manifold and servo fuel injector. Operators of other airplanes, fueled by the same source on the same day, had no indication of fuel contamination.

Probable Cause: loss of engine power for undetermined reasons, and the unsuitable terrain encountered during the emergency landing. A factor in the accident was the pilot's extension of the downwind leg which prevented landing on the intended runway following loss of engine power in the traffic pattern.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA95FA183
Status: Investigation completed
Duration: 3 years and 8 months
Download report: Final report

Sources:

NTSB MIA95FA183

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 13:36 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report]

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