ASN Wikibase Occurrence # 39821
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 10 May 1997 |
Time: | 14:40 LT |
Type: | Piper PA-28R-200 |
Owner/operator: | Riverside Executives, Inc. |
Registration: | N55676 |
MSN: | 28R-7335269 |
Year of manufacture: | 1973 |
Engine model: | Lycoming IO-360-C1C |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Tigard, OR -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Mulino, OR (4S9) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot flew to a local airport for lunch with the passenger. The airplane was full of fuel, and no problems had previously been reported with it. After lunch, the airplane returned to the departure airstrip. During approach, about 1/2-mile from the runway, the engine began to run rough as the airplane was about 200 feet above wooded terrain. The pilot reversed course and attempted a landing in an open field. The airplane struck trees and terrain as the engine began to regain power. The wreckage was subjected to a post-crash fire. Examination of the engine/airframe did not reveal any evidence of preimpact mechanical malfunction. Defoliated trees near the impact site of the left wing indicated the left fuel tank had a significant quantity of fuel at the time of impact. The lack of fuel, fire damage and hydraulic deformation of the right wing, which was found near an area of intense fire, indicated that the right fuel tank was almost empty. The fuel selector valve was found in the RIGHT or OFF position, and it does not have a BOTH selection. The airplane would have consumed more than the max usable capacity of either wing if used exclusively.
Probable Cause: The pilot's failure to properly manage the aircraft fuel supply, which led to fuel exhaustion of the right tank and subsequent fuel starvation/power loss of the engine during the final approach. Factors contributing to the accident were the lack of sufficient altitude to effect a recovery, and the lack of suitable terrain for a successful forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA97FA106 |
Status: | Investigation completed |
Duration: | 2 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB SEA97FA106
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 15:31 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation