ASN Wikibase Occurrence # 40371
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Date: | Friday 21 April 1989 |
Time: | 20:38 |
Type: | Piper J3C Cub |
Owner/operator: | private |
Registration: | N33066 |
MSN: | 5817 |
Total airframe hrs: | 1171 hours |
Engine model: | CONTINENTAL C-85 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ashland, NE -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Weeping Water, NE (EPG) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT AND HIS PASSENGER (WIFE), WHO HAD BEEN SEPARATED FOR SOME TIME, DEPARTED ON A LOCAL FLT FROM WEEPING WATER, NE. ALTHOUGH NOT VERIFIED, THE PURPOSE OF THE FLT WAS BELIEVED TO BE FOR PERSONAL REASONS. LATER, SEVERAL WITNESSES OBSERVEDTHE ACFT FLYING LOW & SLOW OVER THE PLATTE RIVER. A WITNESS NEAR ASHLAND, NE, RPRTD THE ACFT WAS SO LOW THAT THE PLT INITIATED A CLIMB TO CROSS OVER A BRIDGE. WITNESSES LAST SAW THE ACFT FLYING UP THE MEANDERING RIVER (UPSTREAM) AT LOW ALTITUDE. SUBSEQUENTLY, IT WAS FOUND WHERE IT HAD CRASHED IN 3 TO 4 FT OF WATER, ABOUT 30 YDS FROM THE SHORE. THE ACFT CRASHED IN A STEEP NOSE DOWN ATTITUDE, ON A DOWNSTREAM HEADING. THE NOSE OF THE ACFT TOOK THE BRUNT OF THE IMPACT, BUT THERE WAS ALSO DAMAGE TO THE FORWARD COCKPIT, WINGS, WING STRUTS & LANDING GEAR. THE EMPENNAGE & AFT FUSELAGE WERE UNDAMAGED. NO PREIMPACT PART FAILURE OR MALFUNCTION OF THE ACFT WAS FOUND. TOXICOLOGY CHECKS SHOWED THE PLT HAD A URINE/ALCOHOL LVL OF 0.108% & A BLOOD/ALCOHOL LVL OF 0.058%. CAUSE: POOR JUDGEMENT OF THE PILOT BY FLYING WHILE PHYSICALLY IMPAIRED FROM ALCOHOL CONSUMPTION, AND HIS FAILURE TO MAINTAIN ADEQUATE AIRSPEED, WHILE FLYING OVER A MEANDERING RIVER, WHICH RESULTED IN A STALL. A CONTRIBUTING FACTOR WAS THE PILOT'S INADEQUATE ALTITUDE TO RECOVER FROM THE STALL.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X28165 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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