ASN Wikibase Occurrence # 40553
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 20 January 1987 |
Time: | 18:55 |
Type: | Mooney M20C |
Owner/operator: | Abbas Ahmadirmabadi |
Registration: | N3496X |
MSN: | 3427 |
Total airframe hrs: | 3200 hours |
Engine model: | LYCOMING O-360 |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Highgate, VT -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Montpelier, VT (MPV) |
Destination airport: | Montreal,Canada |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACCORDING TO THE SURVIVING PAX, A SNOWSHOWER WAS ENCTRD, SO THE PLT REVERSED COURSE & DIVERTED TO ANOTHER ARPT. DRG A NGT APCH TO LND, THE PAX NOTED A WHITE LIGHT ON THE LEFT SIDE OF THE RWY. (A VASI LIGHT SYS WAS INSTALLED FOR THAT RWY.) THE PLT ABORTED THE LNDG, BUT DRG A GO-AROUND, THE ACFT STRUCK TREETOPS APRX 1500' BEYOND THE DEP END OF THE RWY & CRASHED. NO PREIMPACT PART FAILURE OR MALFUCTION WAS EVIDENT. THE LNDG GEAR & GEAR HANDLE WERE FND IN THE DOWN PSN, THE FLAPS WERE IN A RETRACTED PSN & THE ENG CTLS WERE FND AT FULL POWER SETTINGS. ONLY 3.4 HRS OF THE PLT'S FLT TIME WAS RPRTD IN HI PERFORMANCE OR COMPLEX ACFT & NO ENDORSEMENT TO OPERATE SUCH ACFT WAS FND. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X30141 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation