ASN Wikibase Occurrence # 40842
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Date: | Tuesday 16 May 1995 |
Time: | 19:00 |
Type: | Buccaneer II |
Owner/operator: | private |
Registration: | unreg. |
MSN: | |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Millstone Twsp , NJ -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A WITNESS OBSERVED THE PILOT FLYING HIS TWO PLACE, UNREGISTERED, EXPERIMENTAL HOME BUILT AIRPLANE IN THE LOCAL AREA, AT AN ALTITUDE OF BETWEEN 200 TO 300 FEET AGL. THE WITNESS TURNED AWAY FROM THE AIRPLANE, AND WITHIN ONE MINUTE HEARD THE SOUND OF A CRASH. THE AIRPLANE WAS FOUND IN AN OPEN FIELD WHERE IT HAD IMPACTED IN A NOSE DOWN ATTITUDE, FATALLY INJURING THE PILOT. ACCORDING TO A WRITTEN REPORT FROM THE FAA, EXAMINATION OF THE NUMBER ONE CYLINDER REVEALED, '...SCORING ON CYLINDER WALLS ABOVE THE INTAKE AND EXHAUST PORTS...', AND '...PISTON SCORED ON THE SIDE UP THROUGH THE PISTON RINGS....' ADDITIONALLY, THE PILOT DID NOT POSSESS A PILOT CERTIFICATE OR MEDICAL CERTIFICATE. CAUSE: The loss of engine power due to the seizure of the number one cylinder pistion and the pilot's failure to maintain adequate airspeed which resulted in a stall.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001207X03534 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
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