ASN Wikibase Occurrence # 41145
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Date: | Wednesday 3 June 1998 |
Time: | 18:32 LT |
Type: | Piper PA-30 Twin Comanche |
Owner/operator: | Private |
Registration: | N98NT |
MSN: | 30-927 |
Year of manufacture: | 1965 |
Total airframe hrs: | 3049 hours |
Engine model: | Lycoming IO-320-B1A |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Minor |
Category: | Accident |
Location: | Snohomish County Airport (Paine Field) Everett, Washington -
United States of America
|
Phase: | Standing |
Nature: | Private |
Departure airport: | (KPAE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot taxied the twin engine PA-30 (90 gallon fuel capacity) to a self service fueling island. There, he fueled the aircraft with 58.15 gallons of fuel at 1503. The aircraft was taxied back to the pilot's hangar area. Sometime thereafter, the pilot had used a jumper cable to connect the battery of his car to the aircraft's electrical system at the power receptacle located on the left side of the nose. Approximately 1732, with both engines running, the pilot exited the aircraft to remove the chock from the nose-wheel during which the aircraft rolled forward (east) and eventually impacted a parked Cessna primarily along its leading edge of the right wing. The PA-30's right engine stopped upon wing contact, and the momentum carried both aircraft in a clockwise arc a short distance southeast. The PA-30's left engine continued running after the collision. At a point consistent with the PA-30's initial contact with the Cessna, a pool of blood identified the spot were the pilot was first struck by the PA-30's left propeller. He drug himself under the PA-30 and into a 4:30 position stopping at a point close to the nose-wheel chock which was entangled in the jumper cables. A witness who spoke with the pilot reported that he remarked that 'I knew better, (unknown) was not removed, and the wind caught me.' The pilot was airlifted to a major hospital and expired approximately 10 hours later.
Probable Cause: The pilot-in-command's exiting the aircraft with both engines running to remove a wheel chock. A factor was the inadequate preflight of the aircraft (not removing the chock) prior to engine start.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA98LA085 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB SEA98LA085
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=98NT Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Apr-2017 23:02 |
Dr.John Smith |
Updated [Time, Aircraft type, Operator, Location, Phase, Departure airport, Source, Narrative] |
07-Apr-2017 23:03 |
Dr.John Smith |
Updated [Narrative] |
07-Apr-2017 23:04 |
Dr.John Smith |
Updated [Departure airport] |
07-Apr-2024 11:12 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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