ASN Wikibase Occurrence # 42770
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 9 July 1983 |
Time: | 10:35 |
Type: | Beechcraft N35 Bonanza |
Owner/operator: | private |
Registration: | N1317Z |
MSN: | D-6751 |
Total airframe hrs: | 2791 hours |
Engine model: | CONTINENTAL IO-470-N |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Mccomb, MS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Baton Rouge, LA (BTR) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT CRASHED IN A NOSE LOW ATTITUDE AND WAS DESTROYED. THE TWO PLTS ABOARD HAD BEEN PRACTICING INSTRUMENT APPROACHESAT MCCOMB AND SUDDENLY WITHOUT NOTIFING FSS THE PRACTICE WAS DISCONTINUED TO RETURN TO BATON ROUGE. FSS FOUND OUT ABOUT THE CHANGE BY INITIATING A CALL TO THE ACFT. ABOUT 5 MINUTES AFTER THIS RADIO CALL GROUND WITNESSES OBSERVED THE ACFT CRASH. NO RECORDS WERE FOUND INDICATING FUELING OF THE ACFT SINCE 6/6/83 WHEN 8 GALLONS WAS ADDED. NO EVIDENCE OF FUEL WAS FOUND IN THE ACFT. THE PROPELLER DID NOT INDICATE POWER AT IMPACT. EXAMINATION OF THE THROW OVER COLUMN REVEALED IT WAS IN THE RIGHT POSITION. THE RIGHT SEAT PLT WAS A PRIVATE PLT WITH 195 TOTAL FLYING HOURS. THE LEFT SEAT PLT WAS A COMMERCIAL PILOT WITH 640 HOURS TOTAL FLIGHT TIME. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X43579 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation