ASN Wikibase Occurrence # 42877
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 8 July 1989 |
Time: | 10:55 |
Type: | Beechcraft A45 |
Owner/operator: | West Equipment |
Registration: | N7973A |
MSN: | G-85 |
Total airframe hrs: | 5194 hours |
Engine model: | CONTINENTAL IO-520-BB |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Troy, AL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACCIDENT AIRPLANE WAS THE 2ND OF 5 SIMILAR MODELS PERFORMING A LOW-LEVEL FLYBY OVER THE RWY. WITNESSES REPORTED THAT THE AIRPLANE CLIMBED AND ATTEMPTED TO PERFORM AN AILERON ROLL TO THE LEFT SHORTLY AFTER THE 1ST AIRPLANE HAD SUCCESSFULLY PERFORMED THE MANEUVER. A VIDEOTAPE RECORDING OF THE ACCIDENT REVEALED THAT THE ROLL RATED SLOWED AND THE NOSE BEGAN TO DROP AS THE AIRPLANE ROLLED INVERTED. THE AIRPLANE BEGAN A DIVING TURN TO THE RIGHT, AND SUBSEQUENTLY CRASHED OFF TO THE RT SIDE OF THE RWY. THE WRECKAGE EXAM REVEALED NO EVIDENCE OF ANY PRE-EXISTING MECHANICAL MALFUNCTION OR FAILURE. A RELATIVE OF THE PLT REPORTED THAT THE PLT DID NOT HAVE MUCH AEROBATIC EXPERIENCE AND DID NOT LIKE TO PERFORM AEROBATICS. EXAMINATION OF THE PILOT'S LOGBOOK FOR THE PRECEDING YEAR REVEALED NO LOGGED AEROBATIC EXPERIENCE. A FLY-IN WAS IN PROGRESS AT THE airport WHEN THE MISHAP OCCURRED. ACCORDING TO THE FLY-IN ORGANIZER, NO AERIAL DEMONSTRATIONS WERE PLANNED. CAUSE: THE PILOT'S IMPROPER USE OF THE AIRPLANE FLIGHT CONTROLS DURING A AEROBATIC MANEUVER AT LOW ALTITUDE DUE TO HIS LACK OF AEROBATIC EXPERIENCE. A CONTRIBUTING FACTOR WAS THE PILOT'S OVERCONFIDENCE IN HIS ABILITY TO PERFORM THE MANEUVER.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X28716 ex.USAF/53-3324.
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Feb-2022 17:47 |
A.J.Scholten |
Updated [Source] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation