Accident Thunder And Colt GA42 N28SQ,
ASN logo
ASN Wikibase Occurrence # 43538
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 26 February 1995
Time:16:22 LT
Type:Silhouette image of generic BALL model; specific model in this crash may look slightly different    
Thunder And Colt GA42
Owner/operator:Keith A. Hirsch
Registration: N28SQ
MSN: 1140
Total airframe hrs:1047 hours
Engine model:CONTINENTAL O-200B
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: None
Category:Accident
Location:Hayward, CA -   United States of America
Phase: Approach
Nature:Executive
Departure airport:(KHWD)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE BLIMP HAD A HISTORY OF UNRESOLVED ELECTRICAL SYSTEM CHARGING PROBLEMS. THE GROUND CREW WERE GIVEN RIDES AFTER THE LAST REVENUE FLIGHT. AS ONE OF THE GROUND CREW GOT IN FOR HIS RIDE, HE ACCIDENTLY MOVED THE MIXTURE AND KILLED THE ENGINE. THE PILOT RESTARTED THE ENGINE THEN SAID HE HAD A LOW-BATTERY WARNING LIGHT, BUT THOUGHT HE HAD ENOUGH OF A CHARGE TO MAKE ONE MORE CIRCUIT. THE PASSENGER SAID THE LOW-BATTERY LIGHT REMAINED ON FOR THE ENTIRE FLIGHT. ON APPROACH, THE PILOT WENT AROUND DUE TO A WIND GUST. ON THE SECOND DOWNWIND, THE VOLTAGE DROPPED TO 4 AND THE PILOT TURNED DIRECTLY TOWARD THE LANDING AREA. AT THAT POINT, THE ELECTRICAL SERVOS WHICH MOVE THE CONTROL SURFACES STOPPED WORKING DUE TO THE LOW VOLTAGE. THE BLIMP HIT THE GRASS SHORT OF THE LANDING ZONE AND BOUNCED ALONG THE GROUND UNTIL IT STOPPED NEAR THE TOP OF A BERM. THE PILOT TOLD THE PASSENGER TO GET OUT AND HOLD THE BLIMP DOWN. THE PASSENGER TRIPPED AS HE GOT OUT AND ROLLED DOWN THE HILL. WHEN HE GOT BACK ON HIS FEET, THE BLIMP WAS RISING WITH THE PILOT HOLDING ON TO A HOLD DOWN RAIL. THE PILOT LOST HIS GRIP AND FELL FROM 200 FEET. POSTACCIDENT TESTS OF THE ELECTRICAL SYSTEM REVEALED THAT A SHORT IN THE STARTER SWITCH WAS CONSTANTLY DRAINING THE BATTERY. THE SWITCH WIRING WAS NOT INSTALLED IN ACCORDANCE WITH FACTORY STANDARDS OR THE MAINTENANCE MANUAL.

Probable Cause: the pilot's decision to operate the blimp with a known and unresolved deficiency in the electrical system, which led to a loss of the flight controls and the pilot's improper remedial actions after the blimp came to rest on the ground.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX95LA121
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB LAX95LA121

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 16:29 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Nature, Departure airport, Source, Narrative, Plane category, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org