ASN Wikibase Occurrence # 43713
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Date: | Saturday 11 August 2007 |
Time: | 15:15 |
Type: | Cessna T210G |
Owner/operator: | Private |
Registration: | N225RJ |
MSN: | T210-0287 |
Year of manufacture: | 1967 |
Total airframe hrs: | 2904 hours |
Engine model: | Continental TSIO-520-C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lomita , CA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Torrance, CA (TOA) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane departed from runway 29R, and the flight was cleared to make a right closed traffic pattern to return for landing on runway 29R. On the downwind leg of the traffic pattern, the airplane experienced a loss of engine power, and during the ensuing forced landing, it impacted homes in a residential area. No distress calls were received from the airplane. During recovery of the airplane, approximately 18 to 20 gallons of fuel was drained from the right wing and only a residual amount of fuel was drained from the left wing. No visual evidence of fuel contamination was noted. The fuel selector valve was positioned to the right tank, and the auxiliary fuel boost pump switch was found in the "HI" position. Examination of the airframe and engine did not reveal evidence of any discrepancies that would have prevented normal operation. According to the airplane's Owner's Manual, the fuel boost pump should be switched to "HI" when switching from an empty fuel tank to a tank containing fuel. Apparently the pilot departed with the fuel selector positioned to the almost empty left tank and the engine lost power as a likely result of fuel starvation. The pilot then attempted to restart the engine by switching fuel tanks and turning the fuel boost pump on "HI." The pilot was unable to restart the engine before the airplane impacted the houses. Toxicological testing revealed evidence that the pilot had been taking two different prescription antidepressant medications, bupropion and fluoxetine. Fluoxetine was detected at higher than expected levels in the pilots blood, though it could not be determined if this was due to ingestion of higher than normal amounts of the medication. In typical doses, neither medication would be expected to result in significant impairment, though bupropion is associated with an increased risk of seizure activity, and impairment from the condition for which the medications were prescribed could not be excluded. Neither medication is typically approved by the FAA for use by pilots, and the pilot did not have a current FAA medical certificate.
Probable Cause: The loss of engine power during approach as a result of fuel starvation due to the pilot's improper pre takeoff fuel system selector valve positioning. Contributing to the accident was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA07FA228 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070821X01222&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:49 |
ASN Update Bot |
Updated [Operator, Total occupants, Other fatalities, Destination airport, Source, Narrative] |
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