ASN Wikibase Occurrence # 43882
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Date: | Monday 15 January 2007 |
Time: | 19:43 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Private |
Registration: | N711SK |
MSN: | E-877 |
Year of manufacture: | 1976 |
Total airframe hrs: | 4935 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Wayne, NJ -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Charlotte, NC (CLT) |
Destination airport: | Caldwell, NJ (CDW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane approached the destination airport in night instrument meteorological conditions. The pilot received a clearance for the localizer approach, and radar and global positioning (GPS) data revealed the airplane was established on the localizer course centerline. The airplane crossed the final approach fix 200 feet below the minimum descent altitude (MDA) for the fix, and over the next 1.5 miles, descended on an approximate 7-degree approach angle and a 945 feet-per-minute rate of descent. The airplane continued its descent and struck trees on a ridgeline approximately 400 feet below the intermediate MDA for that segment of the approach. A witness at the crash site saw the airplane through thick fog in a wings-level descent just prior to contact with the trees. She stated that the engine ran smoothly and without interruption. Other witnesses described thick fog along the ridgeline throughout the day prior to the accident, with visibility less than 1/8 mile. Examination of the damaged trees, the crash site, and the airplane revealed signatures consistent with engine power at ground contact. Examination of the wreckage revealed no mechanical anomalies. Post accident flight check results for the localizer approach were "Satisfactory." Further examination of air traffic control (ATC) records revealed that the pilot's first takeoff on the day of the accident was 12 hours prior to the accident.
Probable Cause: The pilot's failure to comply with the published instrument approach procedure, which resulted in controlled flight into terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07FA056 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070123X00088&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:27 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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