ASN Wikibase Occurrence # 45816
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Date: | Saturday 14 July 2001 |
Time: | 13:45 |
Type: | Reitz Mohawk 1 |
Owner/operator: | Private |
Registration: | N109WR |
MSN: | 001 |
Engine model: | Continental O-200 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Camdenton, MO -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Camdenton, MO (H21) |
Destination airport: | Camdenton, MO |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The experimental amateur built airplane was destroyed by impact with a transmission wire, with terrain, and by fire following an in-flight loss of control during climbout. An interview with a witness who had test flown the accident aircraft that morning, noted that, "On the final flight [the witness] found it controllable, but very sensitive to elevator inputs and almost unresponsive to rudder input during flight. [The witness] said he only flew it around the traffic pattern once that morning. ... [The witness] told [the owner] it was OK for taxi, but not safe to fly, and [the owner] departed to taxi it up and down the runway. After some taxiing on the runway, [the witness] observed the aircraft lift-off from runway 15, yaw noticeably to the left, recover and continue climbing out. About 1/2 mile away, he observed it begin a turn to the left, pitch up, stall, and begin a spin to the right. He said it did about 3/4 of a full right spin, disappeared behind trees off the end of the runway and exploded, apparently on impact with the ground." The wind was 140 degrees at 3 knots. The Sheriff's stated, "The craft was located in a field South of [road] 5-120 near Show Me Electrics power lines. ... It appears that the craft struck the ground finally resting on it's top. ... That prior to the craft making contact with the ground it appears that the leading edge of the left wing struck the 'Center Phase' power line approx nine feet from the wing tip."
Probable Cause: The pilot not performing an aborted takeoff and the inadvertent stall he encountered on his inadvertent initial climb. Factors were his inadvertent lift-off, the reported inadequate rudder control, his inadvertent flight with known deficiencies, and the transmission wire.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01LA212 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010726X01522&key=1 Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 11:49 |
ASN Update Bot |
Updated [Departure airport, Source, Narrative] |
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