ASN Wikibase Occurrence # 48454
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Date: | Thursday 6 November 2008 |
Time: | 17:20 |
Type: | Globe GC-1A Swift |
Owner/operator: | Private |
Registration: | N80715 |
MSN: | 118 |
Engine model: | Lycoming O-360-SER |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Ione, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Rancho Murieta, CA (RIU) |
Destination airport: | Rancho Murieta, CA (RIU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the test flight of the experimental airplane, an on-board video camera recorded the takeoff and the pilot activating the landing gear retraction about 2 minutes after takeoff. Approximately 2 1/2 minutes later, the recording showed the pilot's hand slipping from the throttle and his head tilting forward. There were no subsequent coordinated movements made by the pilot, though the airplane remained airborne for about an hour. During this time, the video showed a series of descending and climbing turns varying in altitude between 1,900 feet and 3,800 feet mean sea level (msl). The test flight also included a second airplane, which was also videotaping the test flight. The recorded video from the second airplane verified the same flight path as the recording from the accident airplane. The airborne witnesses observed the accident airplane flying erratically for about an hour before they had to return to the airport due to fuel considerations. During the hour-long flight, the pilot of the second airplane attempted unsuccessfully several times to contact the accident pilot by radio. At one point, the second airplane was able to fly adjacent to the accident airplane. The airborne witnesses observed the accident pilot slumped over the flight controls and unresponsive. The airplane eventually collided with flat open terrain. Post accident examination of the engine found no evidence of a preimpact malfunction. The condition of the pilot's remains did not permit determination of whether the pilot was deceased prior to impact. Toxicology tests of post-mortem samples from the pilot detected alfuzosin, a prescription medication used for the treatment of prostate enlargement. Alfuzosin can rarely result in an unsafe drop in blood pressure, particularly with the first dose, or an increase in dose, but the medication typically does not have any adverse effects, and is routinely approved by the FAA.
Probable Cause: The pilot's incapacitation during cruise for unknown reasons that resulted in a loss of aircraft control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR09LA032 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 12:11 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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