ASN Wikibase Occurrence # 66141
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 3 July 2009 |
Time: | 09:35 |
Type: | Piper PA-30 Twin Comanche |
Owner/operator: | Private |
Registration: | N7657Y |
MSN: | 30-735 |
Year of manufacture: | 1965 |
Total airframe hrs: | 5407 hours |
Engine model: | Lycoming IO-320 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tucson International Airport, Tuscon, Arizona -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Tucson, AZ (TUS) |
Destination airport: | Show Low, AZ (SOW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that after advancing the mixtures to full rich and turning on the fuel boost pumps, he advanced the throttles for takeoff. During the takeoff roll he noticed that the fuel flow on the left engine was a bit excessive. He stated that, as the airplane lifted off the runway at an airspeed of 80 miles per hour, the twin-engine airplane started to veer to the left. Despite the pilot’s control inputs the airplane continued to veer to the left and subsequently impacted the ground, which resulted in structural damage to both wings, empennage, and fuselage. Local law enforcement reported that following the accident the pilot stated that as the airplane was about 30 feet above the ground, “he lost power to the left engine” and was “unable to stabilize the aircraft.” Examination of the left engine revealed that all four top spark plugs were black with soot within the electrode area. The left engine fuel servo was placed on a test bench and was found to be above factory service limitations at a setting consistent with takeoff, which would equate to a slightly rich condition. No anomalies were noted with the examination of the right engine. Examination of the airframe revealed no anomalies that would have precluded normal operation. According to the airframe manufacturer's approved flight manual, the published minimum control airspeed for single-engine operations is 90 mph.
Probable Cause: The pilot’s failure to maintain directional and lateral aircraft control during takeoff. Contributing to the accident was the partial loss of left engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR09LA324 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7657Y 3.
https://flightaware.com/resources/registration/N7657Y Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
04-Jul-2009 00:47 |
slowkid |
Added |
03-Mar-2010 10:42 |
harro |
Updated [Time, Destination airport, Source, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Apr-2017 22:04 |
Dr.John Smith |
Updated [Time, Operator, Location, Departure airport, Destination airport, Source, Narrative] |
02-Dec-2017 15:46 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation