ASN Wikibase Occurrence # 68212
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 12 September 2009 |
Time: | 22:30 |
Type: | Cessna 172S |
Owner/operator: | University of North Dakota |
Registration: | N523ND |
MSN: | 172S10816 |
Year of manufacture: | 2008 |
Total airframe hrs: | 1020 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Park Rapids Airport, Minnesota -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | Park Rapids, MN (PKD) |
Destination airport: | Grand Forks, ND (GFK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot performed a go-around on the first attempted landing at the airport during night visual meteorological conditions. On the second attempt, he landed about mid-field and performed a stop and go landing. He initiated the takeoff using 10-degrees of flaps. The pilot reported that when he reached about 100 feet above ground level, he retracted the flaps. He felt that the airspeed was a little low (70 knots IAS) so he pushed the nose over. He stated that he did not think he was in a descent, but the airplane hit the ground about 100 feet from the end of the runway. The nose gear collapsed and both wings were damaged as the airplane bounced and skidded to a stop. The examination of the accident site revealed eight ground scars in the grass which were consistent with propeller strikes. The propeller blades exhibited leading edge nicks and gouges, chordwise scratching, and blade twist. The inspection of the airplane’s flight controls revealed no preexisting anomalies. The pilot reported that he had 112 hours of flight time with 112 hours in make and model. He had flown 9 hours at night which included 2 hours of night experience when he was pilot-in-command.
Probable Cause: The pilot's failure to maintain a proper climb rate during a night takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN09LA579 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
14-Sep-2009 07:54 |
slowkid |
Added |
15-Sep-2009 05:55 |
RobertMB |
Updated |
15-Sep-2009 05:58 |
RobertMB |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 16:17 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation