ASN Wikibase Occurrence # 69819
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 1 November 2009 |
Time: | 10:40 |
Type: | Bell 206L-1 LongRanger II |
Owner/operator: | Rotorcraft Leasing Company Llc |
Registration: | N272M |
MSN: | 45365 |
Year of manufacture: | 1980 |
Total airframe hrs: | 13668 hours |
Engine model: | Allison 250-C30P |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | In GOM off Galveston, TX -
United States of America
|
Phase: | En route |
Nature: | Offshore |
Departure airport: | HI-A442, GM |
Destination airport: | HI-A515, GM |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter had landed on an off-shore oil platform and was refueled. It then took off with one passenger. Shortly after lifting off, the pilot "heard a loud pop as the nose of the aircraft passed over the edge of the helideck. The noise was simultaneously accompanied by illumination of the engine out warning light and a needle split indication was observed on the engine and rotor tachometer gauge. As the aircraft yawed and lost climb performance, the pilot lowered the collective pitch full down and activated the floats. Upon landing on the water, the aircraft rolled left until inverted. The helicopter was later recovered and the engine disassembled and examined. The only anomaly noted was a loose Pc line, which would cause a loss of fuel flow and subsequent loss of engine power down to or below idle. It was determined that the torque required to realign the B-nut would be between hand-tight and 27 inch-pounds. The required torque is 80 to 120 inch-pounds. Torque values on the other air line fittings between the power turbine governor and the fuel control were found to range from 55 to 85 inch-pounds. A review of the engine maintenance records revealed that 36.7 hours prior to the accident, the turbine module was completely disassembled and overhauled. This would have required the removal and re-installation of the Pc line.
Probable Cause: A total loss of engine power due to maintenance personnel's failure to correctly torque the Pc line following removal and reinstallation of the turbine module.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10LA036 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft
6 June 2006 |
N272M |
Air Logistics |
0 |
South Pass 57, GM |
|
non |
Location
Images:
(c) NTSB
(c) NTSB
Revision history:
Date/time | Contributor | Updates |
05-Nov-2009 03:00 |
RobertMB |
Added |
05-Nov-2009 03:01 |
RobertMB |
Updated |
18-Dec-2009 10:22 |
harro |
Updated |
18-Dec-2009 10:23 |
harro |
Updated |
03-Jun-2012 10:29 |
Anon. |
Updated [Source, Narrative] |
03-Oct-2012 04:28 |
Sidupac |
Updated [Source, Narrative] |
08-Dec-2015 13:19 |
Aerossurance |
Updated [Location, Nature] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 17:48 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation