Accident Beechcraft 35-B33 Debonair N9617Y,
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ASN Wikibase Occurrence # 70038
 
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Date:Tuesday 10 November 2009
Time:17:35
Type:Silhouette image of generic BE35 model; specific model in this crash may look slightly different    
Beechcraft 35-B33 Debonair
Owner/operator:Private
Registration: N9617Y
MSN: CD-583
Total airframe hrs:3774 hours
Engine model:Teledyne Continental IO-470
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:near Chico Airport, CA -   United States of America
Phase: Landing
Nature:Private
Departure airport:Portland-Hillsboro Airport, OR (HIO/KHIO)
Destination airport:Chico Airport, CA (CIC/KCIC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, she filled the fuel tanks prior to departure for the cross-country flight. She switched the fuel selector position every 30 minutes during the flight in an effort to alternate between tanks. She switched to the fullest (left) tank while on approach to the airport. The airplane was on a stable glide path with the gear and flaps down, mixture rich, and propeller at low pitch. On final approach, about 100 feet above ground level, the engine experienced a loss of power. Despite the pilot’s efforts, which included switching to the right tank and turning the fuel boost pump to the "on" position, the engine would not restart. The pilot banked to the right to avoid the runway approach lights and the wing tip subsequently struck the ground, about 200 feet from the runway. The airplane tumbled in a cartwheel-type maneuver before coming to a stop in a nose-down attitude.

First responders observed no fuel in the right wing fuel tank and drained about 12.5 gallons of fuel from the left wing fuel tank. During a postaccident examination, with the airplane in a level attitude, investigators drained 10 gallons of fuel from the right fuel tank and found fuel in the gascolator. Investigators discovered no anomalies that would have precluded normal operation of the airframe or engine.
Probable Cause: A loss of engine power during final approach for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR10LA053
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
11-Nov-2009 00:15 RobertMB Added
11-Nov-2009 05:35 RobertMB Updated
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
02-Dec-2017 17:48 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]
20-Sep-2023 09:25 Ron Averes Updated [[Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]]

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