Accident Cessna 182C Skylane N8948T,
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ASN Wikibase Occurrence # 71864
 
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Date:Saturday 23 January 2010
Time:15:00
Type:Silhouette image of generic C182 model; specific model in this crash may look slightly different    
Cessna 182C Skylane
Owner/operator:Kiley Chandler
Registration: N8948T
MSN: 52848
Year of manufacture:1960
Total airframe hrs:3753 hours
Engine model:Continental O-470 SERIES
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Sparks, Nevada -   United States of America
Phase: En route
Nature:Private
Departure airport:Reno, NV
Destination airport:Reno, NV
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that during cruise flight, he felt a “significant shake” in the airplane and noticed that the engine was losing power. He initiated a precautionary landing to a nearby road. During the descent, the engine failed completely, and despite the pilot’s attempts to restart, the propeller would not rotate. Subsequently, the pilot landed on an unoccupied road. During the landing roll the airplane encountered a ditch and nosed over, which resulted in structural damage to the fuselage, vertical stabilizer, rudder and both wings. Examination of the engine revealed that the number one and two connecting rods separated from the engine crankshaft and exhibited thermal and mechanical damage, consistent with oil starvation. The forward, intermediate, and rear main bearings exhibited signatures consistent with oil starvation. Fragments of the connecting rod bearings were located within the oil sump along with portions of what appeared to be paper towel material. The oil pickup tube was intact and undamaged. The paper-towel-like material was also observed around the oil pickup tube screen and inlet port which restricted the oil flow within the engine. No additional anomalies were noted with the engine. The pilot reported that the engine had accumulated a total time in service of 3,039 hours, with 993 since last overhaul.
Probable Cause: A total loss of engine power during cruise due to oil starvation as a result of foreign material blockage of the oil pickup tube.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR10LA118
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
23-Jan-2010 21:56 slowkid Added
25-Jan-2010 13:01 RobertMB Updated [Time, Aircraft type, Registration, Cn, Operator]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
26-Nov-2017 15:20 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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