ASN Wikibase Occurrence # 72252
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 2 February 2010 |
Time: | 14:00 |
Type: | Bell OH-58A Kiowa |
Owner/operator: | Private |
Registration: | N9286U |
MSN: | 40418 |
Year of manufacture: | 1969 |
Total airframe hrs: | 7580 hours |
Engine model: | Rolls-Royce T63-A-720 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Escalon, California -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Ferry/positioning |
Departure airport: | Escalon, CA |
Destination airport: | Modesto, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had reported to his mechanic prior to the accident flight that the helicopter was not producing full power, was vibrating heavily, and that the DC generator caution light had illuminated. He also reported that his work load was heavy, and that he would continue onwards to return the helicopter to its home base. Shortly after takeoff the engine lost power, the pilot performed a forced landing, and the helicopter collided with terrain. Examination of the engine revealed that a stainless steel pneumatic fuel-to-governor control line had failed at its fitting. Witness marks on the line revealed that it had been rubbing against an adjacent oil line. Additionally, the pneumatic line had been bent during installation such that its surface was in contact with the connector ferrule. Analysis of the line's fracture surface revealed indications of high cycle fatigue. The fuel controller was replaced about 26 flight hours prior to the accident; replacement of the controller would have required the removal and installation of the failed line. The engine manufacturer provided installation guidance in multiple publications, and specifically cautioned against improper installations of engine lines. Examination of the DC starter-generator revealed that it had experienced a partial mechanical failure, which was likely the reason the pilot felt a vibration and observed a dc generator caution light. During the investigation the failed line was replaced, and the engine was successfully run in a test cell throughout its power range.
Probable Cause: A loss of engine power during cruise flight due to the fatigue failure of the pneumatic fuel-to-governor control line. Also causal was the inadequate installation of the pneumatic line by maintenance personnel, and the pilot’s decision to continue flight with a known discrepancy.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA126 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
02-Feb-2010 20:48 |
slowkid |
Added |
03-Feb-2010 10:04 |
Alpine Flight |
Updated [Aircraft type] |
20-Jul-2010 11:04 |
harro |
Updated [Time, Nature, Departure airport, Source, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 15:24 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation