ASN Wikibase Occurrence # 73365
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Date: | Thursday 4 March 2010 |
Time: | 10:30 |
Type: | Enstrom 280FX Shark |
Owner/operator: | Private |
Registration: | N327TB |
MSN: | 2118 |
Total airframe hrs: | 244 hours |
Engine model: | Lycoming HIO-360-51A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 8 mi from Goshen, IN -
United States of America
|
Phase: | Landing |
Nature: | Test |
Departure airport: | Goshen, IN (GSH) |
Destination airport: | Goshen, IN (GSH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter had undergone an annual inspection and was preflighted and flown by the pilot for a maintenance test flight. The pilot did not check the right fuel tank level during that preflight. On the following day, the pilot and another pilot seated in the right seat departed on another maintenance test flight without visually checking the fuel level in either fuel tank. They instead relied on fuel consumption calculations based upon previous flight time and fuel gauge indications. After about 42 minutes of flight time, the helicopter experienced a total loss of engine power while being piloted by the left-seat pilot. The right-seat pilot then took the controls and performed an autorotation but had to maneuver to change the touchdown point in order to avoid power lines. The helicopter then experienced a hard landing. Postaccident examination of the helicopter revealed that there was about one cup of fuel in the left fuel tank and no fuel in the right fuel tank. Postaccident inspection revealed that an electrical connector from the right fuel tank sending unit was found disconnected, which would have given a false "full" indication of fuel quantity.
Probable Cause: The inadequate preflight inspection by both pilots, resulting in a loss of engine power due to fuel exhaustion. Contributing to the accident was the disconnected fuel tank sending unit.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10CA138 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
06-Mar-2010 17:41 |
RobertMB |
Added |
30-Apr-2013 14:32 |
TB |
Updated [Time, Location, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 15:55 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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