ASN Wikibase Occurrence # 195554
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Date: | Sunday 21 May 2017 |
Time: | 13:55 |
Type: | Cessna 182S Skylane |
Owner/operator: | Private |
Registration: | N378ES |
MSN: | 18280013 |
Year of manufacture: | 1997 |
Total airframe hrs: | 2450 hours |
Engine model: | Lycoming IO-540-AB1A5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | West Chester, PA -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Trenton-Mercer Airport, NJ (KTTN) |
Destination airport: | Gaithersburg-Montgomery County Airport, MD (GAI/KGAI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot reported that, about 20 minutes into a cross-country, personal flight, he noticed a loss of oil pressure, Subsequently, he attempted to divert to a nearby airport. The pilot stated that, a few minutes later, the engine began to "shudder," making it difficult to control the airplane, and the oil temperature had increased, so he decided to shut down the engine. The pilot was unable to glide the airplane to the diversionary airport, so he conducted an off-airport landing at a nearby field, during which the airplane struck a utility pole, which resulted in the left wing separating from the airplane.
Examination of the airframe revealed oil streaks along the fuselage belly aft of the engine breather tube. Metal fragments were found trapped in the oil suction screen. About 1/4 quart of oil was present in the sump. Examination of the engine revealed that the crankcase and oil sump were intact, and no indications of oil leaks from the crankcase were found. Thumb compression and suction were established on all cylinders except for the No. 6 cylinder. The No. 6 connecting rod was separated from the crankshaft, and the connecting rod journal and rod end were discolored, smeared, and had gouges, consistent with thermal damage. Remnants of connecting rod bearing material were found loose inside the crankcase. A borescope examination of the remaining cylinders did not reveal any damage or unusual marks.
Based on this evidence, it is likely that an engine crankcase overpressurization occurred, which resulted in the ejection of nearly all the engine oil through the breather tube; the reason for the overpressurization could not be determined. The engine likely began to shudder after the overpressurizaton as a result of the No. 6 cylinder connecting rod failing due to a lack of lubrication.
Probable Cause: An engine crankcase overpressurization and the subsequent loss of engine oil for reasons that could not be determined, which resulted in the failure of the No. 6 cylinder connecting rod due to a lack of lubrication.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA17LA185 |
Status: | Investigation completed |
Duration: | 2 years and 11 months |
Download report: | Final report |
|
Sources:
http://www.philly.com/philly/news/crime/Small-plane-crash-lands-in-West-Chester.html http://www.fox29.com/news/plane-forced-to-make-emergency-landing-in-chester-co https://flightaware.com/live/flight/N378ES http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=378ES NTSB
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
21-May-2017 23:42 |
Geno |
Added |
25-Mar-2022 15:57 |
PolandMoment |
Updated [Destination airport, Narrative] |
27-Mar-2022 18:26 |
Captain Adam |
Updated [Time, Location, Departure airport, Source, Narrative, Category, Photo] |
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