ASN Wikibase Occurrence # 44478
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Date: | Thursday 9 June 2005 |
Time: | 15:41 |
Type: | Beechcraft 76 Duchess |
Owner/operator: | Mvp Aero Academy |
Registration: | N819ER |
MSN: | ME-199 |
Total airframe hrs: | 12684 hours |
Engine model: | Lycoming LO-360-A1G6D |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Conroe, TX -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Conroe, TX (CXO) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 1,000-hour pilot failed to maintain airspeed and lost control of the airplane while attempting to perform a simulated single-engine go-around in a twin-engine airplane. A witness near the approach end of the runway reported observing the airplane moving back and forth in a crab position across the inbound runway course, with the left propeller in the feathered position. A second witness, flying in the traffic pattern behind the accident airplane, reported hearing the pilot report that "he was on a single-engine approach to 14, with a simulated engine out." The witness further stated that as the accident airplane was approximately 20 feet above the middle of the runway, he heard the pilot call out "I'm going around." It was noted by the witness that there was no apparent stress in the tone of the communication, and sufficient distance remained on the runway to land. No emergency transmissions were received from the pilot of the accident airplane. The flaps were found to be in the retracted position at the time of the accident. Examination of the engine and airframe revealed no mechanical anomalies. Examination of the left propeller revealed that the remaining portion of the blade roots and piston were in the feathered position. The governor control lever for the left engine was also found to be in the feathered position. The density altitude was estimated at 2,650 feet.
Probable Cause: The pilot's failure to maintain sufficient airspeed resulting in a loss of control. Contributing factors were the high density altitude, the pilot's improper decision to secure the left engine, and his attempt to perform a single-engine go-around.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW05FA152 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050615X00769&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
06-Dec-2017 10:13 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
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