ASN Wikibase Occurrence # 44525
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Date: | Tuesday 12 April 2005 |
Time: | 17:46 |
Type: | Spearman Raptor |
Owner/operator: | Private |
Registration: | N750TP |
MSN: | TD2-001 |
Total airframe hrs: | 60 hours |
Engine model: | Walter M601E-8 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bogalusa, LA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Daytona Beach, FL (DAB) |
Destination airport: | Bogalusa, LA (BXA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot lost control of the high performance experimental turbo-prop powered airplane on final approach to the airport. About 1.85 miles from the airport, while at an altitude of 852 feet mean sea level (msl), the pilot began a descending right turn for a straight in approach to runway 36 (a 5,000-foot by 100-foot wide runway). Approximately 1,984 feet from the runway threshold, the airplane impacted terrain in a heavily wooded area, came to rest in an inverted position, and was destroyed by post-impact fire. All major components were accounted for at the scene, but due to fire damage a control continuity check could not be performed. An examination of the engine revealed no mechanical defects or anomalies. The 2,000-hour pilot had accumulated a total time of 3-5 hours in the accident airplane. The airplane was a retractable tricycle geared pressurized low-wing prototype of composite construction and had accrued approximately 60 total flight hours since it was manufactured in 2002. The cockpit contained two seats in a tandem arrangement and was equipped with a dual screen Electronic Flight Instrument System (EFIS). During the initial flight test program the airplane revealed several hazardous flight characteristics. The airplane's airframe and engine logbooks were not available for review during the course of the investigation so it could not be determined if any modifications were made to the airplane since the initial test flights were concluded in July 2004.
Probable Cause: The pilot's failure to maintain control of the airplane. A contributing factor was the pilot's lack of experience in the make/model airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW05LA102 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050418X00469&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
06-Dec-2017 08:07 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
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