ASN Wikibase Occurrence # 44530
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Date: | Friday 8 April 2005 |
Time: | 16:00 |
Type: | Stinson 10A |
Owner/operator: | Private |
Registration: | N39482 |
MSN: | 8182 |
Total airframe hrs: | 3128 hours |
Engine model: | Franklin 4AC-199E3 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oak Harbor, WA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Oak Harbor, WA |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A pilot and his passenger flying a Cessna 170 reported that they observed a small airplane on approach, to the east, to a small airstrip. The passenger watched the aircraft on final approach to the point where a go-around was initiated. She was not sure if the aircraft actually touched down or not. She watched it as it pulled up over the trees and continued to the east. She momentarily lost sight of the aircraft due to interference with the frame of the door of the aircraft she was in. When she tried to find the aircraft again, she spotted a plume of smoke. Witnesses near the accident site reported that the aircraft was seen traveling in an easterly direction, very low and near the tree line just before the collision with several trees. The witnesses reported that the engine was running, but seemed like it was strained or not at full power. The local area Paramedic who tended to the pilot before he was airlifted to a hospital reported that he asked the pilot if he had a medical condition, which the pilot responded that he did not. The pilot was also able to recall the day and date and further reported to the paramedic that he "overshot his landing," and that either the "winds or wing flipped him over." At the time of the accident, the winds were from the west at ten knots. During the post-accident inspection of the airframe and engine, no evidence of a mechanical failure or malfunction was found.
Probable Cause: The pilot's failure to adequately plan the approach for landing and maintain clearance from trees during the go-around. A tailwind and trees were factors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA05FA072 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050412X00444&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Oct-2017 20:09 |
TB |
Updated [Aircraft type, Source, Damage] |
06-Dec-2017 08:07 |
ASN Update Bot |
Updated [Operator, Source, Damage, Narrative] |
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