ASN Wikibase Occurrence # 324198
Date: | Thursday 22 May 1997 |
Time: | 14:38 |
Type: | Boeing 767-33AER |
Owner/operator: | Alitalia |
Registration: | I-DEIL |
MSN: | 28147/611 |
Year of manufacture: | 1996 |
Total airframe hrs: | 4917 hours |
Engine model: | General Electric CF6-80C2B6F |
Fatalities: | Fatalities: 0 / Occupants: 168 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Newark International Airport, NJ (EWR) -
United States of America
|
Phase: | Landing |
Nature: | Passenger - Scheduled |
Departure airport: | Milano-Malpensa Airport (MXP/LIMC) |
Destination airport: | Newark International Airport, NJ (EWR/KEWR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Alitalia Flight 600 was approaching Newark (ERW) runway 04R in gusty crosswind, conditions. The pilot received an onboard wind shear alert about 5 seconds prior to touchdown, and the airplane touched down with a 1.8 G load on the main landing gear, followed 2 seconds later by a 2.8 G spike on the nose landing gear. After touchdown, the first officer, the flying pilot, continued to push the control column forward, and the airplane pitched nose down, as the main landing gear alternately lifted off the ground and the ground spoilers retracted.
Examination of the airplane revealed that the nose landing gear trunnions remained attached to the bulkhead that they were affixed to; however, the bulkhead was torn loose from surrounding structure. There were multiple broken stringers and cracked frames, and wrinkled fuselage skin in the vicinity of the nose landing gear. In addition, hydraulic lines were ripped and hydraulic fluid was sprayed into the electronic equipment bay. The cost of repairs was in excess of $20,000,000 US. The accident flight was the first officer's second trip into Newark, and his first trip without a flight instructor onboard; he had 68 hours of flying experience on the B767. The captain had qualified on the airplane about 1 1/2 months prior to the accident flight.
PROBABLE CAUSE: "The improper landing flare by the co-pilot and the inadequate supervision of the flight by the pilot-in-command. Other related factors were the gusty crosswind, windshear, and the lack of familiarity with the airplane by both pilots."
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC97FA098 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB id NYC97FA098
History of this aircraft
Other occurrences involving this aircraft
15 August 2019 |
N378AX |
Omni Air International |
0 |
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|
min |
Aborted takeoff |
Location
Images:
photo (c) Miklos Szabo; Budapest-Ferihegy Airport (BUD/LHBP); 28 April 1999
Revision history:
Date/time | Contributor | Updates |
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