Statuts: | Enquête Officielle |
Date: | vendredi 12 mars 1999 |
Heure: | 07:30 |
Type/Sous-type: |  Boeing 737-377 |
Compagnie: | Ansett Australia Airlines |
Immatriculation: | VH-CZL |
Numéro de série: | 23664/1326 |
Année de Fabrication: | 1986-12-18 (12 years 3 months) |
Moteurs: | 2 CFMI CFM56-3B1 |
Equipage: | victimes: 0 / à bord: |
Passagers: | victimes: 0 / à bord: |
Total: | victimes: 0 / à bord: |
Dégats de l'appareil: | Substantiels |
Conséquences: | Repaired |
Lieu de l'accident: | Melbourne-Tullamarine Airport, VIC (MEL) ( Australie)
|
Phase de vol: | En approche (APR) |
Nature: | Transport de Passagers Nat. |
Aéroport de départ: | Launceston Airport, TAS (LST/YMLT), Australie |
Aéroport de destination: | Melbourne-Tullamarine Airport, VIC (MEL/YMML), Australie |
Détails:At the appropriate time during the approach sequence, the co-pilot of the Boeing 737, who was the handling pilot for the sector, called for the landing gear to be extended. When the pilot in command placed the landing gear lever to the "down" position, a loud thump was heard and the "gear safe" green light for the right main gear illuminated immediately. This was followed by the illumination of the left main and nose landing gear lights, consistent with a normal extension sequence. The aircraft rolled approximately 4 degrees to the right while the gear was extending. This was counteracted by a left roll control input.
As the crew had received indications that the landing gear was safely locked down, they continued the approach and completed a normal landing.
Ramp maintenance staff briefly inspected the aircraft but did not find any immediate cause for the reported thump. The aircraft was then placed on jacks for a retraction test. When the landing gear lever was selected to the "up" position, the right main landing gear moved inboard approximately 15 cm before a grinding noise was heard. The test was immediately suspended and the landing gear was extended.
When access panels were removed, it was found that the actuator beam arm inboard lugs and beam hanger had fractured. The rear wing spar, landing gear beam, aileron bus cable, pulley bracket, aileron and spoiler cables and hydraulic lines had been damaged extensively following the fracture of the lugs and hanger.
Inspection of the actuator beam arm revealed that the fracture of both lugs was due to stress corrosion cracking.
Sources:
» ATSB
Opérations de secours
ATSB issued 5 Safety Recommendations
Issued: 19-MAR-1999 | To: Boeing | IR19990019 |
The Bureau of Air Safety Investigation recommends that Boeing Commercial Airplane Group alert Boeing 737 operators to this safety deficiency and implement an appropriate inspection program. (Closed - Accepted) |
Issued: 19-MAR-1999 | To: Boeing | IR19990020 |
The Bureau of Air Safety Investigation recommends that Boeing Commercial Airplane Group review the effectiveness of Service Bulletin 737-32A1224. (Closed - Accepted) |
Issued: 19-MAR-1999 | To: FAA | IR19990021 |
The Bureau of Air Safety Investigation recommends that the Federal Aviation Administration note the above safety deficiency and interim recommendations and take appropriate action as considered necessary to ensure the integrity of Boeing 737 main landing gear actuator beam arm assemblies. (Closed - Accepted) |
Issued: 19-MAR-1999 | To: CASA | IR19990022 |
The Bureau of Air Safety Investigation recommends that the Civil Aviation Safety Authority initiate appropriate action to ensure that Australian operators of Boeing 737 aircraft immediately inspect all main landing gear actuator beam arm assemblies for evidence of cracking. (Closed - Accepted) |
Issued: 19-MAR-1999 | To: | IR19990023 |
The Bureau of Air Safety Investigation recommends that Australian operators of Boeing 737 note the above safety deficiency and interim recommendations and take appropriate action as considered necessary to ensure the integrity of Boeing 737 main landing gear actuator beam arm assemblies. (Closed - Accepted) |
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Photos
Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Launceston Airport, TAS et Melbourne-Tullamarine Airport, VIC est de 475 km (297 miles).
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.