Accident Rockwell Sabreliner 75A N85DW,
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ASN Wikibase Occurrence # 323449
 

Date:Monday 14 August 2000
Time:18:22
Type:Silhouette image of generic SBR1 model; specific model in this crash may look slightly different    
Rockwell Sabreliner 75A
Owner/operator:Colonels Inc.
Registration: N85DW
MSN: 380-27
Year of manufacture:1975
Total airframe hrs:7185 hours
Engine model:General Electric CF700
Fatalities:Fatalities: 2 / Occupants: 4
Aircraft damage: Destroyed, written off
Category:Accident
Location:5,6 km NE of Ironwood-Gogebic County Airport, MI (IWD) -   United States of America
Phase: En route
Nature:Executive
Departure airport:Brainerd-Crow Wing County Airport, MN (BRD/KBRD)
Destination airport:Flint-Bishop Airport, MI (FNT/KFNT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
A Rockwell Sabreliner 75A, N85DW, was destroyed during a forced landing when it crashed in a densely wooded area northeast of the Ironwood-Gogebic Iron-County Airport (IWD), Michigan. The flight had departed the Brainerd-Crow Wing County Airport (BRD) at 17:47 en route to the Flint/Bishop Airport (FNT), Michigan, on an IFR flight plan.
The pilot received a weather brief that included information concerning a Convective Sigmet and a Severe Weather Watch. The weather briefer informed the pilot that a route to the southeast would keep the flight out of the heavy weather, and that, "... you'll get clobbered if you go due east." After departure, the pilot requested a turn to the northeast to stay clear of weather. While in the climb, the flight was advised of a Weather Watch that covered the area of their flight. The CVR revealed that Continuous Ignition was not selected prior to encountering turbulence.
About 23 minutes after takeoff, the airplane was climbing at about 30,800 feet msl when the pilot radioed a "MAYDAY" distress call, reporting a dual engine failure due to a lightning strike. The CVR indicated one engine quit and the second quit about two seconds later. The copilot established a 170 kts descent airspeed for "best glide."
The airplane was vectored near a level 5 thunderstorm during the emergency descent towards Ironwood. Two air starts were attempted when the airplane's altitude was outside of the air start envelope. Two more air starts were attempted within the air start envelope but were unsuccessful. The minimum airspeed for an air restart is 160 kts and the maximum speed for air start is 358 kts. The CVR indicated that the pilots did not call for the airplane's checklist, and no challenge and response checklists were used during the emergency descent. The CVR indicated the pilots did not discuss load shedding any of the electrical components on the airplane. The CVR indicated the hydraulic system cycled twice during the emergency descent and the landing gear was lowered using the hydraulic system during descent.
The airplane was approximately 17,500 feet msl and 12 nm west of IWD when the pilot reported the airplane lost its navigation capability. The airplane continued its descent toward IWD. The airplane impacted the terrain on an approximate heading of 210 degrees. The pilot and copilot received fatal injuries and the two passengers were seriously injured.

PROBABLE CAUSE: "The pilot's improper in-flight decision, the pilot's continued flight into known adverse weather, the pilot's failure to turn on the continuous ignition in turbulence, and the pilot's failure to follow the procedures for an airstart. Factors included the thunderstorms, the lightning strike, and the woods."

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI00MA256
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

NTSB

Location

Revision history:

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