Date: | Sunday 6 September 2015 |
Time: | 15:30 |
Type: | de Havilland Canada DHC-6 Twin Otter 200 |
Owner/operator: | Rampart Aviation |
Registration: | N181CS |
MSN: | 181 |
Year of manufacture: | 1968 |
Total airframe hrs: | 26915 hours |
Engine model: | Pratt & Whitney Canada PT6A-20 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial, written off |
Category: | Accident |
Location: | Louisburg-North Raleigh Airport, NC -
United States of America
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Phase: | Take off |
Nature: | Executive |
Departure airport: | Louisburg-North Raleigh Airport, NC |
Destination airport: | Louisburg-North Raleigh Airport, NC |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A DHC-6 Twin Otter, N181CS, sustained substantial damage during landing at Louisburg-North Raleigh Airport, North Carolina. The pilot and two passengers sustained serious injuries. Day visual meteorological conditions prevailed and no flight plan was filed for the local business flight.
According to the pilot, the airplane was on the final leg of the traffic pattern when he reduced the power levers in order to descend further for landing, and he noticed that the right engine sounded like "the [propeller] was heading towards beta." The pilot increased the engine power and the sound "went away." Closer to the runway, he decreased engine power and the noise was heard again, the airplane yawed to the right, and he applied left aileron and rudder inputs in order to remain on the runway centerline. Over the runway, the pilot reduced the engine power to idle and the airplane "pushed hard to the right." Then, the pilot applied full power in an attempt to perform a go-around maneuver; however, the airplane yawed about 30 degrees off the runway centerline, the airplane touched down in the grass, and impacted trees prior to coming to rest.
During the accident sequence, the wings and fuselage were substantially damaged.
A postaccident examination of the maintenance logs indicated that an overhauled propeller was installed on the right engine and a test flight was performed on September 4, 2015, which was 8.7 flight hours prior to the accident.
PROBABLE CAUSE: " The propeller's movement to the beta position during landing for reasons that could not be determined during postaccident examination and testing, which resulted in an attempted go-around and subsequent loss of airplane control."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | ERA15LA343 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
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Sources:
NTSB
Location
Images:
photo (c) FAA; Louisburg-North Raleigh Airport, NC; 06 September 2015; (publicdomain)
photo (c) FAA; Louisburg-North Raleigh Airport, NC; 06 September 2015; (publicdomain)
photo (c) Adrian Romang; Hawassa, Ethiopia; 07 November 2013
photo (c) via Werner Fischdick; Lanzarote Airport (ACE/GCRR); December 2009
Media:
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Revision history:
Date/time | Contributor | Updates |
11-Dec-2023 10:40 |
harro |
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