Runway excursion Accident Learjet 31A PP-BBV,
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ASN Wikibase Occurrence # 319063
 

Date:Saturday 2 January 2021
Time:11:51 UTC
Type:Silhouette image of generic LJ31 model; specific model in this crash may look slightly different    
Learjet 31A
Owner/operator:Brasil Vida Táxi Aéreo
Registration: PP-BBV
MSN: 31-113
Year of manufacture:1995
Engine model:Garrett TFE731
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial, written off
Category:Accident
Location:Diamantina Airport, MG (DTI) -   Brazil
Phase: Landing
Nature:Ambulance
Departure airport:São Paulo-Congonhas Airport, SP (CGH/SBSP)
Destination airport:Diamantina-Juscelino Kubitschek Airport, MG (DTI/SNDT)
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The Learjet 31A suffered a runway excursion after landing on runway 03 at Diamantina Airport, Brazil. It went down a dropoff.
The aircraft was operating an ambulance flight to pick up a Covid-19 patient.

Diamantina Airport has a single asphalt runway (03/21), measuring 1610 x 30 m. Past the paved runway surface of runway 03 there is a 60 m stopway, followed by downsloping terrain.

Contributing factors:
- Application of controls - contributed.
Considering that the distance ahead of the aircraft at the moment of touchdown (600 m) was not sufficient to decelerate and stop the plane within the runway limits, it was found that an inadequacy in the use of flight controls led to a long landing, where, from the touchdown point, there was not enough runway to safely stop the aircraft.
- Attitude - undetermined.
The fact that the PIC (PM) had already conducted several flights with the SIC (PF) without any issues, as well as their close relationship, may have contributed to an attitude of excessive confidence and resulted in a non-assertive perception of the approach parameters during this phase of the flight.
- Cockpit coordination - contributed.
The account of the events leading up to the landing indicated that the available human resources for aircraft operation were not adequately utilized, as the PIC (PM) only noticed the deviations that led to this runway excursion on short final, characterizing inefficient cockpit coordination as a contributing factor to the studied accident.
- Fatigue - undetermined.
Based on the medical examinations conducted after the accident, as well as the overall picture observed by the medical representative, it was inferred that the lack of response from the SIC (PF) to the PIC's (PM) alerts and impairment to his alertness could be indicative of the pilot experiencing fatigue-related effects that may have interfered with his performance.
- Perception - contributed.
The attempt to land even in the face of an unstable approach characterized an inadequate perception of the risks involved in continuing this procedure under the experienced conditions.
- Pilot judgment - contributed.
The decision to proceed with the landing, even after conducting an unstable approach to a position where only 600 m of runway would remain for the aircraft to stop, as well as the failure to consider the alternative of a go-around, characterized an inadequate judgment regarding the risks of the operation conducted under the circumstances.

Accident investigation:
cover
  
Investigating agency: 
Report number: A-001/CENIPA/2021
Status: Investigation completed
Duration: 2 years and 11 months
Download report: Final report

Sources:

g1.globo.com
itatiaia.com.br

Location

Images:


photo (c) Corpo de Bombeiros Militar de Minas Gerais; Diamantina Airport, MG (DTI); 02 January 2021


photo (c) Corpo de Bombeiros Militar de Minas Gerais; Diamantina Airport, MG (DTI); 02 January 2021

Revision history:

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