ASN Wikibase Occurrence # 122533
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Date: | Wednesday 18 May 2011 |
Time: | 11:15 |
Type: | Bellanca 17-30A Super Viking 300A |
Owner/operator: | Mickey Gilmer |
Registration: | N93577 |
MSN: | 73-30591 |
Total airframe hrs: | 4632 hours |
Engine model: | Continental IO 520 K |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | South Pass area, between Farson and Rock Springs, Wyoming -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Pinedale, WY (KPNA) |
Destination airport: | Fort Collins, CO (KFNL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot’s initial plan was to make the cross-country flight on the day before the flight actually took place. But, since the weather briefing he received forecast clouds, precipitation, and icing conditions along much of the route, the pilot elected not to attempt the flight but instead decided to wait until the next day. Although the weather briefer advised the pilot that the conditions he had described would still be present along the route of flight the next day, including areas of clouds, low ceilings, precipitation, icing conditions, snow, and thunderstorms, the pilot did not call back for an update briefing on the day of the flight, and he did not receive a weather briefing from either of the Direct User Access Terminal Service providers. It is possible that he may have accessed some raw weather data from a National Oceanographic and Atmospheric Administration website before departing for his planned destination. Overlaying the airplane’s radar track on weather radar imagery indicated that, about 30 minutes after departure, the pilot encountered the edge of the forecast weather conditions, entering an area of precipitation where supercooled liquid droplets had been forecast. This most likely resulted in a very rapid accumulation of ice on the airplane’s structure, including its wings and horizontal stabilizer. Soon thereafter, the airplane entered a steep uncontrolled descent, during which the outboard section of the right wing separated as it was stressed beyond the design limitations of the airplane. The airplane continued in a near vertical uncontrolled descent and impacted the terrain with a high amount of energy. Postaccident examination of the airframe, flight controls, and the engine did not find any evidence of a preexisting anomaly.
Probable Cause: The pilot’s decision to continue flight into an area of known adverse weather, which resulted in an accumulation of structural ice that led to a loss of control and in-flight breakup. Also causal was the pilot’s inadequate preflight weather planning.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR11FA228 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
20-May-2011 04:01 |
RobertMB |
Added |
20-May-2011 04:13 |
RobertMB |
Updated [Aircraft type] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 16:55 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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