ASN Wikibase Occurrence # 131649
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Date: | Friday 1 November 1991 |
Time: | 19:06 LT |
Type: | Cessna 172N |
Owner/operator: | Thief River Aviation |
Registration: | N8283E |
MSN: | 17272169 |
Engine model: | Lycoming 0320H2AD |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bemidji, MN -
United States of America
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | Thief River Fls, MN (TVF |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT OF A SINGLE ENGINED AIRPLANE HAD JUST RECEIVED AN IFR CLEARANCE. THE AIRPLANE PERFORMED AN INTERSECTION TAKEOFF AT NIGHT WITH WINDS GUSTING TO 30 KNOTS AND BLOWING SNOW. JUST PRIOR TO ROTATION THE PILOT STATED HE OBSERVED THE AIRSPEED INDICATOR DISPLAYING '0'. HE DECIDED TO TAKEOFF BECAUSE HE BELIEVED INSUFFICIENT RUNWAY REMAINED FOR AN ABORTED TAKEOFF. AFTER TAKEOFF THE PILOT STATED HIS OTHER PRESSURE INSTRUMENTS WERE NOT FUNCTIONING PROPERLY. THE AIRPLANE COLLIDED WITH TREE AND TERRAIN APPROXIMATELY 2 MILES FROM THE AIRPORT'S CENTER. THE ON SCENE INVESTIGATION REVEALED A SLIGHT TRACE OF ICE WAS ON THE WINGS LEADING EDGE. ONE OF THE TWO STATIC PORTS WAS FOUND WITH ICE BLOCKING IT. THE SECOND STATIC PORT WAS DESTROYED DURING THE CRASH SEQUENCE. THE ALTERNATE STATIC SOURCE SWITCH WAS FOUND IN THE 'STANDBY' POSITION. THE PILOT STATED, 'I FIGURED I COULD USE THE ALTERNATE STATIC SOURCE ONCE I WAS UP HIGH ENOUGH TO CLEAR THE TREES.'
Probable Cause: INADEQUATE PREFLIGHT PLANNING AND PREPARATION BY THE PILOT IN COMMAND, THE NON PERFORMANCE O FAN EMERGENCY PROCEDURE AND NOT MAINTAINING A POSITIVE RATE OF CLIMB ON BEHALF OF THE PILOT IN COMMAND. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE PILOT IN COMMAND'S NOT REMOVING ICE FROM THE AIRPLANE, NOT OBTAINING ALTITUDE DURING THE CLIMB, AND NOT MAINTAINING DIRECTIONAL CONTROL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI92LA021 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB CHI92LA021
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
11-Apr-2024 11:27 |
ASN Update Bot |
Updated [Time, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report] |
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