Accident Beechcraft G18S N38RM,
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ASN Wikibase Occurrence # 131660
 
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Date:Wednesday 4 December 1991
Time:05:05 LT
Type:Silhouette image of generic BE18 model; specific model in this crash may look slightly different    
Beechcraft G18S
Owner/operator:Viking Express
Registration: N38RM
MSN: BA-574
Year of manufacture:1961
Engine model:P&W R-985-14B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:West Chicago, IL -   United States of America
Phase: Initial climb
Nature:Unknown
Departure airport:
Destination airport:Covington, KY (KCVG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT STATED SHE FELT THE TWIN ENGINED TAILWHEEL CARGO AIRPLANE YAW TO THE RIGHT DURING TAKEOFF. THE PILOT STATED SHE APPLIED LEFT RUDDER AND SET DIFFERENTIAL POWER TO CORRECT FOR THE PERCEIVED RIGHT HAND CROSSWIND. AS THE AIRPLANE LIFTED OFF, IT MADE A SHARP RIGHT TURN AND PERFORMED LEFT AND RIGHT BANKS LEVELING OFF PRIOR TO COLLIDING WITH THE GROUND. THE AIRPLANE SLID THROUGH SECURITY FENCES AND A FUEL SUPPLY DEPOT BEFORE STOPPING. THE NEWSPAPER BUNDLE CARGO MOVED FROM THE TWO FORWARD BAYS TO THE AFT END OF THE CARGO COMPARTMENT. THE NEWSPAPERS WERE COVERED WITH PLASTIC WRAPPER. THE CARGO COMPARTMENT FLOOR WAS SLIPPERY WHEN WALKED UPON AND HAD TRACES OF SNOW ON IT. ACCORDING TO THE PILOT THE CARGO WAS COVERED BY A CARGO NET SECURED AT THE FORWARD END BUT NOT AT THE AFT END. TWO CARGO STRAPS WERE CRISSCROSSED OVER THE NET AND SECURED AT THE AFT END OF THE CARGO LOAD. THE LEFT THROTTLE WAS FOUND IN THE FULL FORWARD POSITION. THE RIGHT THROTTLE WAS FOUND ONE INCH AFT OF THE FULL FORWARD POSITION.

Probable Cause: A RESULT OF THE PILOT IN COMMAND'S NOT MAINTAINING DIRECTIONAL CONTROL, AN IMPROPER INFLIGHT DECISION, AND IMPROPER REMEDIAL ACTION ONCE THE LOSS OF DIRECTIONAL CONTROL WAS RECOGNIZED BY THE PILOT. FACTORS CONTRIBUTING TO THIS ACCIDENT ARE INADEQUATE CARGO RESTRAINTS, LOOSE CARGO, AND IMPROPER SECURITY OF THE CARGO NOT OBSERVED BY THE PILOT. ADDITIONAL FACTORS CONTRIBUTING TO THIS ACCIDENT ARE THE INADEQUATE STANDARDS FOR AIRCRAFT EQUIPMENT AND TRAINING PROVIDED BY THE COMPANY EMPLOYING AND OPERATING THE AIRPLANE.

Accident investigation:
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Investigating agency: NTSB
Report number: CHI92FA037
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB CHI92FA037

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
11-Apr-2024 11:02 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report]

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